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Consolidated XB2Y

Type of aircraft From Wikipedia, the free encyclopedia

Consolidated XB2Y
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The Consolidated XB2Y was an American prototype single-engined dive bomber of the 1930s. It was intended to meet a United States Navy requirement for a carrier-based dive bomber, but was unsuccessful, only a single example being built.

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Design and development

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In 1932, the United States Navy issued a specification for a two-seat carrier-based dive bomber capable of carrying a 1,000 lb (450 kg) bomb.[1] Orders were placed for competing prototypes of designs to meet the Navy's requirement with Consolidated Aircraft and the Great Lakes Aircraft Company in June 1932.[2][3]

Consolidated's proposal was the Model 24 (or XB2Y in the US Navy's designation system), a single-bay biplane developed from a basic design prepared by the Navy's Bureau of Aeronautics with detailed design led by Consolidated's B Douglas Thomas,[2] formerly Chief Designer of Thomas Morse Aircraft, which had become part of Consolidated Aircraft in 1929.[4]

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In order to withstand the high g-forces experienced during pullup after a dive attack, much of the aircraft's center-section was cut from a solid steel block.[2][5] It was powered by a similar Pratt & Whitney R-1535 Twin Wasp Junior air-cooled radial engine as used by the Great Lakes design,[2][3] and had a fixed tailwheel undercarriage. The crew of two sat in tandem in separate cockpits, with the observer in the rear cockpit armed with a single flexibly mounted machine gun, and the pilot with a single fixed synchronized machine gun firing through the aircraft's propeller arc. Its bombload was carried on a crutch under the fuselage that swung down to ensure the bomb would clear the propeller when dropped in a steep dive.[2]

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Operational history

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The prototype XB2Y-1 (serial number 9221[6]) was completed in 1933, being delivered on 28 June 1933.[2] Testing was unsuccessful,[2] with the aircraft's performance being unsatisfactory,[7] while the aircraft also proved very expensive to build.[2][5] The US Navy preferred the Great Lakes design, with 60 being ordered as BG-1s.[3]

The XB2Y-1 was modified to a scout configuration, removing the bomb crutch. This allowed it to reach a height of 23,400 ft (7,100 m),[2] and it was used by NACA at Langley, Virginia for pilot view tests.[8]

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Specifications (XB2Y-1)

Data from General Dynamics Aircraft and their Predecessors[9]

General characteristics

  • Crew: two
  • Length: 27 ft 11 in (8.51 m)
  • Wingspan: 36 ft 6 in (11.13 m)
  • Height: 10 ft 10 in (3.30 m)
  • Wing area: 362 sq ft (33.6 m2)
  • Empty weight: 3,538 lb (1,605 kg)
  • Gross weight: 6,255 lb (2,837 kg)
  • Powerplant: 1 × Pratt & Whitney XR-1535-64 14-cylinder air-cooled radial engine, 700 hp (520 kW)

Performance

  • Maximum speed: 158 kn (182 mph, 293 km/h) at 8,900 ft (2,700 m)
  • Range: 423 nmi (487 mi, 784 km)
  • Service ceiling: 22,800 ft (6,900 m)
  • Time to altitude: 10 minutes to 12,200 ft (3,700 m)

Armament

See also

Aircraft of comparable role, configuration, and era

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References

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